Indeed we are are thankful this stupid action by an Amtrak crew did not result in serious accident. Had 14 not been ao late at that point, the results may have been much different.Glad that everybody, self included, made it safe and sound even if there were inconveniences involved. Of course when I got off at PDX - two hours late - there was somebody who didn't get off if K Falls who thought she was entitled to a hotel room and passage on tomorrow's Builder; "she's on her own" is what I overheard - and rightly so.
What's really troublesome is the seriousness of the Surfliner's running the red. If we and they ended up in the same block going opposite directions, what's to keep something awful from happening? Fortunately some backup system or something kept us safe. Is this area under some sort of positive train control?
At any rate, I'm sure the engineer and conductor - regardless of the drug test results - are in deep trouble. And the fact that it worked out makes me more confident that I'll never awake to find my sleeper a pile of twisted metal.
In all at least 3 trains were significantly affected and three train loads of passengers were inconvienineced by this "incident". And yet I have seen nothing on the Amtrak page appologing or taking responsibility. This was a serious incident and Amtrak owes all of its customers an explanation of what happened and what actions were taken as a result. Once folks are back from the new year holiday I will contact customer relations and likely write Mr. Boardman. This was a serious incident and will likely be swept under the rug.
Stan